While some details may have changed since this case study
was undertaken, the principles and the positive outcomes, both
financial and environmental, remain the same and are transferable
to any business.
Scholle
Industries
Company profile
Scholle Industries Pty Ltd (Scholle) is the Australian subsidiary
of the Scholle Corporation and specialises in the manufacture
of flexible packaging. It has its headquarters in Adelaide and
employs around 260 staff. Scholle was initially established to
meet the needs of the wine industry but has since expanded to
other segments of the food industry.
Manufacturing processes
Scholle manufacture a range of sizes in the bag-in-box
container market from 2 L through to 1,500 L. There are four main
processes within the Scholle plant.
Plastic injection moulding of fittings
The majority of bag fittings are made using injection-moulding
techniques.
Film extrusion
Flexible packaging is produced using a plastic resin is
extruded to a film
Lamination
Some of the extruded films are laminated with a metallised
polyester, before being assembled in the bag room
Bag Making
The bag making room houses a patented process that assures high
level of production quality.
Link
to Yalumba
Scholle supply Yalumba with bag in a box packaging.
This is generally delivered in bulk bins which each contain approximately
2,000 bags.
Action undertaken
An eco-efficiency audit was conducted at Scholle in March 2002
that inspected and reviewed the company facilities and activities.
This included assessment of the:
- Supply chain (transportation and logistics)
- Inputs including energy usage (electricity, gas), and water
usage
- Outputs including waste generation, and products
Several eco-efficiency initiatives were identified during the
program and were included into an Action Plan including:
- Reduced waste in various manufacturing processes, and
- Reduced energy consumption.
The following table provides a summary of the Action Plan.
| AREA |
ACTION |
POTENTIAL BENEFITS |
| Bag Room |
Reduce waste generation using new technology.
Bag Room light fittings. |
Less waste materials, reduced waste to landfill. New 28
W light fittings can provide the same output as older 30 or
40W fittings. |
| Air conditioning |
Air conditioning set point increased. |
Reduced electricity costs. |
Slitter
|
Reduce waste generation, investigate potential recycling
options |
Less waste materials, reduced waste to landfill. |
| Clean Room |
Install quick response roller door. |
Reduced air loss from clean room area and reduced wasted
energy. |
| Chiller System |
Use of variable speed drives on the pumps and a primary/
secondary loop. |
Possible energy saving of 35% - 45% of current running costs.
|
| |
Use of higher efficiency water cooled chillers rather then
air cooled. |
|
| |
Use of chilled water temperature reset. The set point of
the chilled water could be increased from 6 degrees on light
load days to say 9 degrees. |
|
| |
Integrating the chilled water system so that a new higher
efficiency centrifugal chiller could be installed in lieu
of a reciprocating system. |
|
Project outcomes
As a result of the project Scholle has received direct cost savings
and identified the following specific outcomes:
Environmental benefits
Modifications have been made to bag room machine and have already
achieved waste reduction targets. Total waste to landfill is trending
down. A Victorian recycler is recycling some plastic waste material.
Air conditioners controls adjusted, reducing energy consumption.
Economic benefits
Reduced waste generation has produced cost savings of $15,000/year,
which is being invested to plant trees (100,000) to replace CO2
the company produces.
Other issues that have arisen include:
items outlined in the Action Plan were not completely implemented.
Areas have been identified for electricity usage improvement and
actions implemented, however modifications to machine 13 have
been separated into three stages.
Scholle intends to install power factor correction device for
the chiller system, however the use of variable speed drives does
not appear feasible. There has been an overall downward trend
in electricity consumption, possibly due to increased employee
awareness.
This page was last modified 23-10-2007
|